Investigation of the Internal Flow in a Francis Turbine for Comparing the Flow Noise of Different Operation Conditions
Abstract
:1. Introduction
2. Research Object
3. Mathematical Methods
3.1. Basic Equations
3.2. Turbulence Model
3.3. Flow-Induced Noise Analysis
4. Setup of CFD
5. Comparison of Experimental and Numerical Results
6. Results of CFD
6.1. Streamlines
6.2. Flow-Induced Noise
6.2.1. Reference Planes for Plotting
6.2.2. Contours of Flow-Induced Noise
6.2.3. The Variation in Flow-Induced Noise with Flow Direction
7. Discussion
8. Conclusions
- (a)
- The main locations where flow-induced noise occurred included spiral case inlets, runner blade inlet edges, draft tube walls, and the middle of the draft tube. The flow-induced noise was closely related to the flow convergence and extrusion, fluid–blade interaction, draft tube rotating flow, etc. The noise caused by the interaction between the fluid and high-speed rotating runner was often the strongest;
- (b)
- Flow-induced noise was related to the operation condition. When the turbine was operating in the allowed region (point one), the noise was lower. When the turbine was operating in the restricted region (point two) and the prohibited region (point three), the noise was higher. An exception occurred in the region near the vanes, as it was mainly affected by the opening of the guide vanes;
- (c)
- The difference in sound power level was related to the flow regime. When swirling flow was strong, it could cause high noise. When flow was smooth, the induced noise was low. In addition, flow-induced noise was not significant when flow was obstructed. In contrast, when the flow passed through the guide vanes at high speed, the flow-induced noise was strong.
Author Contributions
Funding
Data Availability Statement
Acknowledgments
Conflicts of Interest
References
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Parameter | Value |
---|---|
Rotor diameter Drn | 5.80 m |
Rated output power Pr | 183.7 MW |
Rated flow rate Qr | 301 m3/s |
Rated rotation speed nr | 100 r/min |
Rated head Hr | 68.0 m |
Maximum output power Pmax | 204.1 MW |
Turbine installation height Hins | 895.00 m |
Component | Grid Element Number |
---|---|
Spiral case | 209,260 |
Stay vane | 558,230 |
Guide vane | 623,824 |
Runner | 897,680 |
Draft tube | 464,692 |
Total | 2,753,686 |
Point | CFD Efficiency | Experimental Efficiency | n11 | Q11 |
---|---|---|---|---|
Point One | 91.05% | 90.51% | 77.85 | 0.7864 |
Point Two | 71.72% | 70.32% | 78.55 | 0.3678 |
Point Three | 55.25% | 52.88% | 91.21 | 0.3495 |
Symbol of Position | Position Description |
---|---|
A | At spiral case inlet |
B | Between stay vane and guide vane |
C | In runner blade channels |
D | Near runner cone in draft tube |
E | Middle of draft tube straight section |
F | Near draft tube elbow section |
G | In draft tube diffusion section |
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Zhang, T.; He, G.; Guang, W.; Lu, J.; Song, X.; Zhu, D.; Wang, Z. Investigation of the Internal Flow in a Francis Turbine for Comparing the Flow Noise of Different Operation Conditions. Water 2023, 15, 3461. https://doi.org/10.3390/w15193461
Zhang T, He G, Guang W, Lu J, Song X, Zhu D, Wang Z. Investigation of the Internal Flow in a Francis Turbine for Comparing the Flow Noise of Different Operation Conditions. Water. 2023; 15(19):3461. https://doi.org/10.3390/w15193461
Chicago/Turabian StyleZhang, Tao, Gensheng He, Weilong Guang, Jiahao Lu, Xijie Song, Di Zhu, and Zhengwei Wang. 2023. "Investigation of the Internal Flow in a Francis Turbine for Comparing the Flow Noise of Different Operation Conditions" Water 15, no. 19: 3461. https://doi.org/10.3390/w15193461
APA StyleZhang, T., He, G., Guang, W., Lu, J., Song, X., Zhu, D., & Wang, Z. (2023). Investigation of the Internal Flow in a Francis Turbine for Comparing the Flow Noise of Different Operation Conditions. Water, 15(19), 3461. https://doi.org/10.3390/w15193461