2.1. Background
Penrhyn Castle is a historical tourist attraction receiving >200,000 visitors annually on average. The castle comprises extensive grounds, historic buildings and a café serving hot food and drinks with associated hot water consumption for food preparation and cleaning. Penrhyn Castle was chosen as an optimum location for heat recovery, considering it involved significant use of hot water in various activities. The hot water consumption during peak tourist season at the Castle is about 1000 m
3 on a monthly basis, which justifies the scope for WWHR investigations (See
Figure A1).
The Tearooms, in particular, were selected for installation of the pilot plant following an extensive wastewater heat resource monitoring campaign at different locations within the Castle’s sewer network (See
Section 2.2).
Figure 1 illustrates an aerial view of the Castle and some of the surrounding grounds, including the approximate location of the sewer network, heating system and pre-installation resource monitoring points.
Wastewater generation from the Tearooms kitchen is seasonal, with more tourists visiting the Castle in the summer period (see
Figure A1). The Castle is closed during parts of the winter but has a year-round hot water demand from the on-site staff of the operator. The site was also chosen to help reduce the carbon emissions of a historic building and to improve the sustainability of heritage preservation in line with the site operator’s objectives. Deep energy retrofits are often not possible in protected structures like this one, and thus, WWHR can play an important role in improving its carbon footprint. This is achieved through the capture and recycling of heat embedded in wastewater flushed down the drain and wasted to the environment prior to the installation of the pilot.
The current primary heating system is located in a biomass building (plant room), 250 m away from the Castle and at an elevation of about 30 m lower than the Castle (see
Figure 1). Reducing heat consumption at the Castle would result in less biomass consumption and also reduced pumping costs for the main heating loop. The property is currently heated by two woodchip-based biomass boilers of 150 kW each (total 300 kW), represented as the traditional heating system in
Figure A2 in
Appendix A. The heat produced by the boilers is collected by a primary heating loop. The heat is then delivered to the secondary loop, also denoted as the main heating loop, by a plate heat exchanger. This is represented by the dashed lines in
Figure 1 from the biomass building to the technical room local to the tearoom kitchen.
The following sections outline the details of the heat recovery system design and results obtained from the data monitored at the Penrhyn Castle Tearooms to show the thermal performance and payback period for operational and economic feasibility, respectively.
2.2. Wastewater Heat Resources Monitoring Campaign
The first stage in the design of a WWHR system was to assess the available waste heat resources and predict the feasibility (technical and economic) of installing the system at differing locations within a sewer system. Thus, a wastewater heat resources monitoring campaign was first carried out over several months in 2017 and 2018 to record wastewater flows and temperatures and assess technical viability in differing locations (e.g., distance between wastewater heat sources and the building’s heating system).
The rural location of Penrhyn Castle means it relies on a system of septic tanks to manage its wastewater. These are located a distance from the main castle at a lower elevation (see
Figure 1). In line with the findings of Nagpal et al. [
16], the assessment of the wastewater heat resources at Penrhyn Castle was conducted to measure the available heat at the hot water application level, whole building level, sewer level, and within the wastewater treatment facility. In this case, the wastewater treatment facility was in the form of a series of large septic tanks. Therefore, as shown in
Figure 1, monitoring of wastewater heat was conducted at the septic tanks, at the intermediate junction within the sewer network and the discharge point from the kitchen within the Castle. The heat resources were expected to have the highest flow volumes at the septic tanks, while the highest temperatures were expected to be located closer to the Castle. An assessment of which location contained the optimum balance of high energy and lower installation costs was the object of the measurement campaign.
Table 1 illustrates the location, measurement type, period and frequency, and measurement devices used in the monitoring campaign. The Tinytag TG-4100 (Gemini Data Loggers (UK) Ltd., West Sussex, UK) records temperatures between −40 °C to 70 °C with an accuracy range of 0.5–0.75 °C above 0 °C and was used at locations 1 and 3a–c. The hot and cold water flow rates at location 1 were taken from meters internal to the Penrhyn Castle existing systems. The temperature and flow rates for location 2 were measured using an ATEX MSFM sensor flow monitor (Dectronic Limited, Lancanshire, UK) where the accuracy was ±0.5% and ±2.5%, respectively.
Initially, the location labelled as Option 2 in
Figure 1 was selected for heat recovery resource monitoring. This location contained three settlement or septic tanks. These were Klargester-type tanks with two large (9000 L) units for the collection of wastewater from the Castle and one smaller unit (4500 L) for the collection of the wastewater from the visitor toilets, which can be seen as the small building adjacent to Option 2, in
Figure 1. With sufficient heat resources and a WWHR system, incoming cold water to the Castle could be preheated here and sent to the biomass boiler building a short distance away (see
Figure 1).
The distance between the WWHR source and the location where these heat savings can be integrated within the existing heating system is an important factor in the viability of WWHR systems. The longer this distance is, the more expensive it will be to lay pipework and perhaps provide pumping to connect the two systems. In addition, the longer this distance is, the greater the system losses will be where recovered heat is lost to the environment. The three septic tanks and biomass boilers were located at a similar elevation, which would avoid the need for additional pumping in this case, which was seen as an additional advantage to this location.
The tanks comprised an inner chamber for solid matter to settle and an outer chamber for wastewater accumulation. The wastewater temperature data collected showed a maximum of 13 °C during the 12-month sampling campaign, as illustrated in
Figure A3 in
Appendix A. This relatively low temperature meant that WWHR was unjustified at this location due to too high heat losses in the 250 m distance between the main Castle building and the septic tanks. In addition, evidence of groundwater infiltration within the sewer system at the mid-point acted to increase ambient heat losses further.
In parallel to this, monitoring was also conducted at the intermediate junction in the sewer network halfway between the septic tanks and Castle (see
Figure 1). At this location, it was hoped that ambient heat losses could be reduced while wastewater volumes would be maintained. Unfortunately, negligible thermal differences persisted here due to ambient losses and groundwater infiltration. Thus, our monitoring campaign moved ahead towards Option 1, which is at the outlet of the Tearoom in the Castle.
The monitoring of drain water temperatures at the kitchen drain resulted in temperatures up to 58 °C, with median values ranging from 22–38 °C and an average daily flow of around 650 L (see
Figure 2). The hot and cold water consumption within the kitchen was collected in order to account for drain water flow. This data was also used by Spriet et al. (2019) to generate synthetic load profiles for daily variations in wastewater flows and temperatures [
8]. This was potentially an ideal location for heat recycling as the discharge point was in very close proximity to the heating interface unit (HIU) between the biomass boiler and the main castle heating loop (a 2–3 m distance). Therefore, recycled heat could be more easily integrated into the existing heating system at this point.
These conditions provided the opportunity for a direct heat recovery system whereby the waste heat is recovered using a heat exchanger only, and this heat was of sufficiently high temperature to avoid the need for a heat pump [
16]. For these reasons, Option 1, at the kitchen drain, was selected as the pilot site. The temperature of the drain water is sufficiently elevated to directly preheat the mains water using the pilot heat recovery system (see
Figure 3).
2.3. Option 1 Pilot System Design
Option 1, the direct heat recovery method, requires a heat exchanger, associated pipework components, and, in case the mains pressure is insufficient, a pump to circulate clean water through the heat exchanger. A direct buffer tank was also installed to store the preheated water, having a capacity of 300 L (see
Figure 3a), to provide a consistent preheated water supply during the non-operational hours of the kitchen. Spriet et al. (2019) highlighted that a temporal mismatch exists between the generation of hot wastewater and the demands for hot water use and that WWHR system efficiency and economic viability could be improved in this regard by incorporating a buffer tank within the system to store saved heat [
5]. The pilot system, in this case, incorporating a direct buffer tank, preheats the mains source water using the concentric shell and tube-type heat exchanger, and therefore, the required heat from the conventional heating system is reduced, resulting in a decrease in fuel consumption, related costs and emissions.
The WWHR set-up was situated in a technical room where flow and temperature data were collected. This housed the buffer tank for storage of preheated water, an HIU, and a concentric shell and tube type high thermal conductivity copper drain pipe heat exchanger arrangement to achieve WWHR (see
Figure 3). The two main locations of the WWHR system are: 1. Heat recovery from kitchen wastewater coming down the drain to preheat the cold freshwater (via a heat exchanger, see
Figure 3b), and 2. HIU (see
Figure 3c and
Figure A4), where hot water from the biomass boiler is indirectly exchanged with the preheated water from the WWHR system to supply freshwater at the desired temperature to the Tearooms.
The hydraulic installation of the WWHR system was first performed using copper components, and in a later stage, these were insulated against ambient heat losses using a lagging material (see
Figure 3b). A commercially available concentric shell and tube counter flow heat exchanger was used to replace the kitchen drain, as shown in
Figure 3b. The heat exchanger comprised a 168 cm long concentric pipe, 50 mm waste pipe diameter, with a capacity of 50 L/min of drain water and two 15 mm diameter freshwater connections. The wastewater flow could easily accommodate the flow rates shown in
Figure 2b and was also matched to the existing 50 mm wastewater pipework. In the design stage, the effectiveness of the heat exchanger was estimated at 58%, taken as a weighted average from the manufacturer’s freshwater flow rate data (See
Appendix A Figure A4). This estimated effectiveness was taken as a weighted average of the expected effectiveness based on the manufacturer’s information and the flow estimations in the drain of the kitchen at the tourist attraction in Wales. An interactive post-installation 3D view of the pilot installation can also be viewed at
https://dwruisce.github.io/PenrhynE/ (accessed on 1 September 2022).
The energy supplied for water heating was derived from a woodchip-based biomass boiler. The pilot WWHR system was installed and placed in operation in Feb 2022 and operated for the full 2022 tourist season (February–September) to harness heat from the Tearooms at Penrhyn Castle. Continuous monitoring has been conducted to record temperature and freshwater flow at regular intervals at various locations of the installed unit to evaluate the amount of heat recovered, as shown in
Figure 3c.
The logging and visualisation of data collected were provided by Detectronic and installed on-site after the installation of the hydraulic system. For data storage and monitoring, three transmitters were installed on site (see
Figure 3a), collecting data in 10-minute intervals. The wastewater heat recovery system temperatures were monitored using PT-100 temperature sensors with an accuracy of ±0.30 °C at 0 °C (RS Pro, London, UK), which recorded temperature data at the top (
TT) and bottom (
TB) of the heat exchanger (HX) in the buffer tank (
TBT), in the cold water supply (
TS), and ambient air temperature (
Ta). Freshwater circulation in the HX flow circuit was maintained via a circulation pump (Grundfos Alpha 2L). The freshwater flow rate from the HX was measured using a flow sensor with an accuracy of ±1% (RS Pro Liquid Acetal Copolymer 4.5–16 V dc sensor, RS Pro, London, UK) and calibrated to provide 0.027 kg/s.
The system performance was assessed in terms of the magnitude of waste heat saved and recycled in the building’s heating interface. The buffer tank accommodates preheated water received from the heat exchanger and compensates for the time lag between hot wastewater generation and demand for hot water consumption. A time lag exists between when the heat is recovered and when it is required for supplementing hot water use. The direct buffer tanks enable the storage and optimisation of the recovered resources. Freshwater circulated continually through the concentric shell and tube heat exchanger ensures that the buffer tank always supplies preheated water during usage. A heating interface unit supplies additional heat from the main heating loop to further boost the preheated water from the buffer tank to the desired temperature. The HIU itself comprises another heat exchanger whereby heat recovered and stored in the BT is indirectly exchanged with heat provided by the Castle’s main heating loop (provided by a biomass boiler). The incoming freshwater feed was preheated and stored in the buffer tank before it reached the heat interface unit. The HIU provides the interface which indirectly exchanges the thermal energy from the hot water generated by the biomass boilers and transported in the main heating loop with the preheated water from the WWHR system (see
Figure A5 of
Appendix A). The presence of the WWHR system results in a higher temperature for the freshwater going into the HIU. Therefore, the water requires less energy to reach a desired temperature of 60 °C.
In the case of the Tearooms at Penrhyn Castle, the distance between the HX at the kitchen drain, the buffer tank location, the HIU, and the existing heating loop is approximately 2–3 m. Buildings with larger distances between WWHR resource location and the location of the existing heating system would require additional capital investment not required here, which in some cases could make WWHR unviable. This paper investigates the case for economically viable recovery of wastewater heat using existing heat exchanger technology and new design configurations of the full system layout, considering all required system components. The paper examines whether the significant potential for energy and CO2 emissions savings that exist for buildings with significant hot water usage can be exploited in practice.
2.4. Mathematical Expressions Used in Performance Analysis
The power needed to raise the temperature of cold freshwater from the supply temperature to the desired temperature level, i.e., generally 60 °C, was determined according to Equation (1). Equation (2) determines the power required in the HIU to heat freshwater to the desired temperature when the pilot heat recovery system is active/operational. No heat recovery took place during periods when no hot wastewater was discharged to the drain (e.g., at night-time when the Tearooms were closed or in winter periods).
The following mathematical expressions were used to determine the energy-saving performance of the system over time:
where
is the desired hot tap water temperature, which is considered 60 °C,
denotes freshwater supply temperature,
denotes preheated water stored in the buffer tank,
is the freshwater mass flow rate in the HX, and
Cp is the specific heat capacity of water. The power saved due to the installation of the pilot waste heat recovery system is given as:
Missing data during the monitoring campaign occurred on a number of occasions due to sensor failure at the
TB location and due to challenges with remote connectivity. In these cases, the missing data was predicted according to the measured relationship between
TB,
TT and
TBT. This relationship was found to follow Equation (4) with an
R2 adjusted of 87% based on 16,866 simultaneous measurements of all three variables. Less than 10% of data recordings contained missing values:
The Payback period (
calculations were based on the cost of energy saved on an annual basis and are given as:
The pilot heat recovery system total cost was £1885, which comprised of an arrangement of concentric copper heat exchanger pipe (£495), a water pump (£364), a buffer tank (£400), labour cost (£525), and cost for additional piping materials (£100). The cost of the data monitoring and telemetry system is not included here as this would not be required in a commercial installation. Similarly, the cost of human resource time in the design of the system by the research team was also not included, and in a commercial system, this would be accounted for in a markup of the profit margin. As such, payback periods estimated here are based on the cost–price only and are an underestimate of the commercial cost.
The cost of energy saving was based on the rates of differing fuel types in the UK for the years 2021 and 2022, as shown in
Table 2 [
20,
21]. While biomass was the actual fuel used on site, the impact of differing fuel types on payback was assessed as the provision of water heating using biomass in the hospitality sector is not a very common form of heating in the UK.
Greenhouse gas (GHG) emission savings calculations were based on the expression given as:
Additionally, GHG emissions are associated with the production of 1 kWh of electricity, considered as 0.28307 kg CO
2e/kWh [
5].