Investigation of Hydraulic Performance and Arrangement Optimization of Non-Prismatic Water Conveyance Tunnel—A Case Study of Project X
Abstract
:1. Introduction
2. Experimental Method
2.1. Project Profile
2.2. Experimental Setup
2.3. Similarity Theory
- Discharge scale:
- Velocity scale:
- Time scale:
2.4. Design of Experiment
3. Numerical Simulation
3.1. Geometric Model
3.2. Governing Equation
4. Results
4.1. Validation of Free Flow
- (1)
- Flow pattern
- (2)
- Flow rate
- (3)
- Water surface profile
4.2. Hydraulic Discrepancy of Submerged Flow
- (1)
- Flow rate
- (2)
- Velocity along the centerline
4.3. Hydraulic Performance in Contraction Section of Submerged Flow
- (1)
- Pressure in the contraction section
- (2)
- Wind velocity
4.4. Prevention Measures
- (1)
- Scheme design
- (2)
- Flow rate
- (3)
- Pressure in contraction section
5. Conclusions
- (1)
- For free flow, the flow characteristics, such as flow pattern, flowrate, and water surface profile, showed good agreement between the experimental results and the simulation predictions; this indicated that the numerical simulation effectively aligned with the experimental scale model test data when assessing the hydraulic performance of a water conveyance tunnel with a contraction section under free flow conditions.
- (2)
- For submerged flow, notable deviations of the flow rate and velocity in non-prismatic tunnels emerged. The primary factor behind this divergence was the development of a vacuum within the distorted cross-sectional area caused by the presence of the contraction section, and the similarity theory proved inadequate for predicting the hydraulic performance during scale model tests.
- (3)
- In order to figure out the applicability of the scale model test and numerical simulation for forecasting the flow state, the hydraulic performances in the contraction section of the submerged flow were analyzed; the results of the pressure and wind velocity verified the inadequacy of the similarity theory in non-prismatic tunnels and indicated the reliability of the simulation method.
- (4)
- The reason for the failure of the scale model test in non-prismatic tunnels is that the vacuum created within the distorted cross-sectional area and the contraction section can be promptly released through the gate shaft. As the vacuum propagates upstream, it gives rise to water entrainment phenomena within the reservoir, which consequently leads to an increase in the flow rate.
- (5)
- To mitigate the adverse effects of negative pressure on both cavitation damage and the hydraulic performance within the tunnel, the placement of the gate shaft was optimized. The vacuum issue was settled in the distorted plan section, and the numerical simulations agreed well with the scale model test. These findings not only validated the accuracy of the CFD analyses, but also substantiated the applicability of the modified design for implementation in water conservancy projects.
Author Contributions
Funding
Data Availability Statement
Conflicts of Interest
References
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Flow Regime | Operating Conditions | |
---|---|---|
Upstream Flow Depth in Scaled Model for Experiment (Model Scale Is 1:50) | Upstream Flow Depth in Prototype Model for Simulation | |
Free flow | 0.01 m | 0.5 m |
0.02 m | 1.0 m | |
0.03 m | 1.5 m | |
0.04 m | 2.0 m | |
0.05 m | 2.5 m | |
0.06 m | 3.0 m | |
0.07 m | 3.5 m | |
0.08 m | 4.0 m | |
Submerged flow | 0. 10 m | 5.0 m |
0.12 m | 6.0 m | |
0.14 m | 7.0 m | |
0.16 m | 8.0 m | |
0.18 m | 9.0 m | |
0. 20 m | 10.0 m | |
0.22 m | 11.0 m |
Upstream Flow Depth (m) | Discharge (m3/s) | Relative Deviation | |
---|---|---|---|
Experimental Value | Simulation Value | ||
0.5 | 1.79 | 1.71 | −4.46% |
1 | 4.78 | 4.99 | 4.39% |
1.5 | 9.15 | 8.92 | −2.51% |
2 | 12.82 | 13.73 | 7.10% |
2.5 | 18.21 | 18.67 | 2.52% |
3 | 23.32 | 25.15 | 7.85% |
3.5 | 30.92 | 31.68 | 2.49% |
4 | 36.80 | 38.67 | 5.08% |
Upstream Flow Depth (m) | Discharge (m3/s) | Relative Deviation | |
---|---|---|---|
Experimental Value | Simulation Value | ||
5 | 52.3 | 56.06 | 7.19% |
6 | 71.19 | 78.28 | 9.96% |
7 | 78.58 | 85.56 | 11.43% |
8 | 85.35 | 97.84 | 14.63% |
9 | 95.12 | 109.69 | 15.32% |
10 | 101.77 | 118.98 | 16.91% |
11 | 108.43 | 127.89 | 17.94% |
Flow Regime | Elevation Head | Discharge (m3/s) | Relative Deviation | |
---|---|---|---|---|
Experimental Value | Simulation Data | |||
Free flow | 0.5 | 1.68 | 1.70 | 1.41% |
1.0 | 4.77 | 4.93 | 3.42% | |
1.5 | 8.76 | 8.93 | 1.94% | |
2.0 | 13.52 | 13.08 | −3.24% | |
2.5 | 18.57 | 18.73 | 0.88% | |
3.0 | 24.93 | 25.25 | 1.27% | |
3.5 | 31.42 | 30.31 | −3.53% | |
4.0 | 38.29 | 37.31 | −2.56% | |
Submerged flow | 5.0 | 51.52 | 52.31 | 1.53% |
6.0 | 65.53 | 65.95 | 0.63% | |
7.0 | 76.32 | 77.67 | 1.77% | |
8.0 | 82.21 | 87.88 | 6.90% | |
9.0 | 89.07 | 97.17 | 9.10% | |
10.0 | 95.63 | 106.24 | 11.09% | |
11.0 | 101.98 | 114.28 | 12.06% |
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Li, S.; Yuan, Q.; Zhao, Y.; Cui, H.; Su, X.; Peng, A.; Zhang, Y. Investigation of Hydraulic Performance and Arrangement Optimization of Non-Prismatic Water Conveyance Tunnel—A Case Study of Project X. Water 2024, 16, 311. https://doi.org/10.3390/w16020311
Li S, Yuan Q, Zhao Y, Cui H, Su X, Peng A, Zhang Y. Investigation of Hydraulic Performance and Arrangement Optimization of Non-Prismatic Water Conveyance Tunnel—A Case Study of Project X. Water. 2024; 16(2):311. https://doi.org/10.3390/w16020311
Chicago/Turabian StyleLi, Songping, Qun Yuan, Yuliang Zhao, Hongtao Cui, Xiaoyu Su, Ao Peng, and Yisheng Zhang. 2024. "Investigation of Hydraulic Performance and Arrangement Optimization of Non-Prismatic Water Conveyance Tunnel—A Case Study of Project X" Water 16, no. 2: 311. https://doi.org/10.3390/w16020311
APA StyleLi, S., Yuan, Q., Zhao, Y., Cui, H., Su, X., Peng, A., & Zhang, Y. (2024). Investigation of Hydraulic Performance and Arrangement Optimization of Non-Prismatic Water Conveyance Tunnel—A Case Study of Project X. Water, 16(2), 311. https://doi.org/10.3390/w16020311