4.1. Design and Implementation of Grouting Boreholes
In the study area, the No. 4 aquifer is known for its relatively shallow burial depth, measuring an average of 270 m, along with its irregular thickness and intricate lithology. The weathering zone of the underlying bedrock varies significantly in thickness, ranging from 4.5 m to 45.6 m, with a prevailing range of 15 m to 25 m and an average value of 22 m. Additionally, there is a pronounced strong weathering zone with a thickness ranging from 0.41 m to 37 m, averaging about 13 m. In response to the challenges posed by these geological conditions [
24], squeezing and splitting grouting techniques have been employed to create a consolidated layer with a fixed skeleton within the No. 4 aquifer, as shown in
Figure 6. This process reduces the water saturation of the reformed strata, transforming the aquifer into a weakly water-rich or nearly drained Class III water body. Simultaneously, this grouted treatment enhances the overall strength of the No. 4 aquifer, thereby mitigating the risk of sudden water–sand mixture inrush [
25] during underground mining operations. Moreover, this approach facilitates the extraction of resources from the shallow coal pillars. On the basis of the grouted treatment of the No. 4 aquifer, it is recommended to extend the grouted drill holes into the weathering zone of the bedrock to reinforce this zone. This proactive step aims to prevent water–sand mixture inrush incidents during underground mining activities, ultimately ensuring the safety and stability of such operations.
The construction process involves the utilization of the vertical boreholes arranged row by row to disperse the water and consolidate the sand. The boreholes, as indicated in
Figure 7, have specific structural features. The first section of boreholes, extending approximately 25 m above the bedrock surface, has a hole depth of around 245 m and a diameter of 215.9 mm. These boreholes are encased in a Φ177.8 × 8.05 mm casing and cemented. The second section of boreholes features with a diameter of 152 mm, with downstream segmented grouting governance and a unit section length of 4 to 6 m. Finally, the third section of boreholes extends to approximately 10 m below the top surface of the bedrock.
The grouting project implemented a segmented downstream approach, utilizing both the orifice-closed static pressure grouting method and the orifice stopping method [
26]. It incorporates a combined grouting process that combines continuous and intermittent grouting techniques. The No. 4 aquifer and the weathering zone of the bedrock are both the primary targeted layers for grouting. In terms of materials, the grouting mixture comprises the general silicate P.O 32.5 cement and fly ash obtained from coal-fired power plants.
The drilling, coring, grouting parameters, and operations adhered to the design specifications, yielding satisfactory results throughout the construction process. By 10 March 2021, the on-site drilling and grouting activities were completed after 191 days, encompassing the completion of 42 boreholes. A cumulative drilling length of 11,790.03 m, with coring of 243.03 m, and a total of 336 scans of boreholes were conducted. In addition, inclination measurements for boreholes spanned 11,790.03 m, accompanied by 44 pressure water tests. The installation of casing required 365.880 tons of cement, while the overall grouting volume for the No. 4 aquifer and the weathering zone of the bedrock reached 70,267 tons, comprising 57,742 tons of cement and 12,525 tons of fly ash [
27].
Post-assessment after grouting confirmed that the checking boreholes from ground met the designated requirements. The grouting spread radius, which exceeded 50 m, demonstrated a diffusion effect that was more satisfactory than expected. Notably, the water influx from each checking boreholes did not surpass 0.5 m3/h, aligning with the anticipated effectiveness of the project.
4.2. Field Detection after Being Grouted
The analysis for the feasibility of grouting the No. 4 aquifer based on the field project is presented in
Figure 8. The overall grouting ability was measured at 50.8 t/m; with the injectability, it was reduced to 47.7 t/m when excluding the pre-existing grouting holes Z3 and Z4. The unit grouting amount of the coring inspection boreholes averaged 15.9 t/m. However, for boreholes J4, B1, and B2, the unit grouting amounts were 19.2 t/m and 43.6 t/m, respectively, with an average of 26.8 t/m. It is important to note that after grouting, the injectability of the inspection boreholes was significantly less than the overall injectability. The middle and lower sections were more injectable than the upper section, as shown in
Figure 9.
The compressive strength of the samples from the weathering zone of the bedrock ranged from 3.03 to 11.10 MPa, significantly exceeding that of the bedrock section in the cored borehole before grouting, which ranged from 1.96 to 2.18 MPa. The grouting treatment enhanced the strength of the weathering zone of the bedrock by approximately 2 to 5 times. Compared to the test results of the cored borehole samples before being grouted, there was a slight increase in the true density and an slight improvement in the overall compressive, tensile, and shear strengths. Additionally, a marginal decrease in water content was observed in the samples following grouting.
According to the water pressure test data obtained from the boreholes, it was determined that the water permeability of the core boreholes decreased significantly after grouting compared to before the grouting process. Prior to the treatment, a pumping test was carried out on borehole Z12, followed by tests on boreholes J4 and B1 post treatment. The results from these tests allowed for the derivation of the hydrogeological parameters for the test section, which revealed that the No. 4 aquifer within the grouting area generally displayed a low water-yielding characteristic overall.
Upon entering the No. 4 aquifer, it was noted that the drilling holes were prone to collapsing and jamming, as reported in the underground disclosure. While water was initially present in the No. 4 aquifer, the water flow dwindled rapidly to 0 m3/h in some boreholes, with others showing a complete absence of water. These observations suggest that the No. 4 aquifer had transitioned into a weakened aquifer state.
Samples of the water-bearing sand of the No. 4 aquifer were collected from the boreholes for analysis. The samples revealed a significant presence of cement, indicating the extensive spread of grouting slurry over a considerable distance into the No. 4 aquifer. Analysis of the 27 underground inspection boreholes indicated a diffusion radius of ≥51 m during grouting, with the 1#, 2#, and 3# inspection boreholes exhibiting a diffusion radius of ≥71 m during grouting. Furthermore, sampling and analysis of the weathering zone demonstrated that the cement spread to considerable depths during grouting, effectively enhancing the strength of the bedrock. The results from the 27 underground inspection boreholes illustrated the significant transformation effect of grouting, successfully extruding water from the No. 4 aquifer within the grouting section and solidifying the sand layer as intended.
4.3. Simulation of Similar Materials in Trending and Dipping Directions before/after Being Grouted
The study focused on analyzing the impact of grouting on the stability and integrity of structures in geo-technical engineering and underground mining projects. To achieve this, a simulation of the engineering geo-mechanical model was conducted to investigate the development of fissures, displacement, and stress evolution of the roof overburden during the mining progression of the No. 10 coal seam in the 1010-1 panel of the Wugou coal mine. The model, illustrating the mining progression from right to left, is depicted in
Figure 10, showing two engineering geo-mechanical models for the trending profile. One model represents the No. 4 aquifer and the weathering zone without grouting, while the other model corresponds to the grouting condition.
Excavation in the No. 10 coal seam within the trending profile resulted in varying heights in the grouted and ungrouted areas, reaching 4.2 m and 4.6 m, respectively (
Figure 10). The advancement of the panel caused stress disruptions within the quarry, leading to the initiation and upward development of cracks [
28]. In the grouted area, the caving zone expanded to a height of 15.2 m, while the water-conductive fracture zone extended up to 56.6 m without fully penetrating into the No. 4 aquifer.
Additionally, the No. 3 aquiclude clay layer, which overlays the No. 4 aquifer and possesses better plasticity and a greater thickness, did not significantly impact the aquifers above it. Moreover, on the left side of the ungrouted area (
Figure 10e,f), where the coal seam is buried deeper with an overburden thickness exceeding 40 m and the mechanical properties of the rock layer are superior, the overall damage was less compared to the right side (
Figure 10c,d). The measured height of the caving zone in this area was 18.6 m, with the height of water-conductive fracture zone being approximately 42.6 m, which was lower than that observed in the thinner bedrock area.
In the model, as shown in
Figure 10b, the trending profile advanced to the left from the opening cut on the right side of the model. Once the panel was fully mined out, the caving zone and water-conductive fracture zone were basically developed and stabilized. The weathering zone, post grouting, displayed minor fractures, exhibiting significantly reduced overall damage compared to the ungrouted model, as depicted in
Figure 10d,f. There were absciss layers at the bottom boundary of the No. 3 aquiclude, and the other absciss layers gradually tended to close. In the ungrouted model (
Figure 10f), the caving zone reached a height of approximately 20.3 m after the completion of mining operations, with the water-conductive fracture zone extending up to 62.4 m, penetrating into the No. 4 aquifer. Following grouting (
Figure 10d), the model forecasted the caving zone of the trending profile of the panel after mining to range from 16.4 m to 20.2 m in height, accompanied by a water-conductive fracture zone measuring 53.4 m [
29].
Stress measurement points in the trending and dipping profile were designed and are shown in
Figure 11.
Figure 11b depicts the stress variation curves along the survey line at various advanced distances within the trending profile. The model indicates that the original stress equilibrium state of the overburden rock was disrupted upon the excavation of the panel from the opening cut. With the advancement of the panel, the stress state of each measurement point along measurement line 1 underwent continuous alterations, with the stress value following a pattern of “stable–slowly rising–suddenly falling–stable”. Similarly, measurement line 5 demonstrated incremental changes in the stress values at each measurement point, with an overarching trend of “rise–fall–balance” changes. In comparison to the stress change pattern observed in line 1, certain measurement points in line 5 manifested a more moderate stress variation trend. This moderation can be attributed to the distance from the mining area and the presence of an overlying loose layer, resulting in a more moderate stress change trend within this region.
The stress evolution curves before and after being grouted revealed that the stress fluctuations at each measurement point were reduced to varying degrees post grouting. Moreover, the stress difference between the initial stress equilibrium state and the final equilibrium state decreased. This mitigation of the stress concentration indicates an improvement in the engineering properties of the weathering zone of the bedrock and No. 4 aquifer, leading to increased strength.
Figure 11c shows the stress variation curves of the survey line at different advanced distances in the trending profile. The No. 4 aquifer forms a stable skeleton structure, which can, to a certain extent, share the load of the upper loose layer and transfer it to the areas on both sides of the quarry, thereby reducing the degree of stress concentration at each measurement point.
To monitor the evolution of roof displacement during mining, a camera was employed to observe the vertical displacement at each measuring point of the displacement-coded measuring line [
30]. These observations were then simultaneously combined with the calibration of the rope-pulled displacement sensor to mitigate errors generated by the manual measurements, as illustrated in
Figure 12a.
During the initial stages of mining, cracks propagated upwards along the quarry, continuously intersecting with the direct roof strata. This led to the gradual deterioration of the direct roof, which exhibited a tendency to collapse downwards. Upon completion of the panel advance, the caving zone and the water-conductive fracture zone became essentially developed and stabilized. This process is illustrated in
Figure 12b, which depicts the dynamic evolution of the displacement of each line of measurement at different advanced distances in the trending profile. As a result of these developments, the emergence of a “double peak” phenomenon in the top plate sinking curve can be observed.
Figure 12c depicts the dynamic evolution of the displacement of survey lines at various advanced distances for the grouted and ungrouted trending profiles. The displacement of the middle measurement points was slightly greater than that of the measurement points on both sides of the model. This observation aligns with the “saddle-shaped” destruction of the roof overburden following mining activities. This tendency was consistent with the progression of the model from right to left. Compared with the displacement change curve of each measurement point in the ungrouted model, the displacement change of each measurement point after being grouted was slightly slower. After the grouting treatment of the No. 4 aquifer, the displacement of each measurement point decreased to varying degrees. Furthermore, as the quarry displacement stabilized, each measurement point in the ungrouted model entered a phase of smooth fluctuations of the displacement. This transition indicates an increase in the internal strength of the aquifer after the grouting treatment, consequently resulting in a slower trend of destruction of the overburden rock.
The phenomenon of a gradual decrease in displacement at measurement points further away from the quarry in the vertical direction can be partly attributed to the development of absciss layers, which were not completely closed. This gradual decrease was also influenced by the crushing and swelling of broken rock, as they can fill void areas and fissures. Consequently, the displacement of the measurement point decreased as the distance from the quarry increased, reflecting the combined effect of these factors [
31].
4.4. Numerical Simulation of Trending and Dipping Profiles before/after Being Grouted
Figure 13a presents a cloud view of the quarry displacement upon completion of the trending profile. In the pre-mining stage, grouting produced a beneficial effect on controlling the fractures of the rock formation and reducing displacement. The range of large displacement areas in the grouting model was significantly smaller than that in the ungrouted model, as shown in
Figure 13c,d. Notably, through the opening cut and the left side of the stopping area, it was evident that the displacement-affected area in the ungrouted model was considerably larger [
32]. This highlights that grouting into the No. 4 aquifer can effectively reduce the displacement around the panel, thereby reducing the subsidence area scope.
Figure 13b presents a cloud view of the quarry displacement upon completion of the dipping profile. At the end of the simulated panel, the caving zone and water-conductive fracture zone were significantly developed and stabilized throughout the quarry. In the displacement cloud of the ungrouted model, the area with a larger displacement change was noticeably larger compared to the range of the grouted model on the right side, as shown in
Figure 13c,e. This indicates that the overall displacement of the ungrouted model on the left side was relatively larger, which is basically consistent with the results observed in the model test. Furthermore, the subsidence level of the overlying rock of the ungrouted model was larger than that of the grouted model, and the degree of destruction was more severe [
33].
In the early stage of mining, the model showed that as the panel advanced from the left side, the original stress equilibrium state of the rock was disrupted, leading to a redistribution of the stress field in the overburden. The stress distribution in the entire quarry exhibited a “landing funnel” pattern [
34], which extended from the upper part of the open area to the model boundary. The upper part of the open area showed a parabolic pattern of stress reduction, while the two sides of the open area showed prominent concentration zones, indicated by light green coloring.
Figure 14a presents a cloud view of the quarry stress upon the completion of the trending profile. In the ungrouted model, as the panel progressed, the mudstone layer above the basic and key stratum was visibly broken, leading to stress release. Conversely, in the grouted model, there was an improvement in the geo-technical properties of the overlying weathering zone and the No. 4 aquifer. This enhancement is shown in
Figure 14c,d where the No. 4 aquifer formed a stable “skeleton” structure within the zone, effectively preventing damage and disruption to the overlying strata. With the grouting treatment, the roof damage exhibited a degree of hysteresis when compared to the ungrouted model. Subsequently, after the completion of the panel, the roof strata made contact with the coal seam floor, resulting in the re-generation of stress connections.
Figure 14b depicts a cloud view of the quarry stress at the end of the dipping profile. As the panel progressed, the “landing funnel” extended towards the overlying No. 3 aquiclude. It was observed that the stress fluctuation state of the quarry remained essentially unchanged before and after being grouted, as noted by previous research [
35]. A significant contrast, however, was evident in the reduction in the maximum compressive stress of the quarry after grouting in comparison to pre-grouting conditions, as shown in
Figure 14c,e. In the middle section of the mining area, a stress concentration area formed due to the bending and sinking of the overlying strata. After the completion of the panel mining and stabilization to a steady state, there was a noticeable similarity in the distribution of stress figures in the quarry before and after being grouted.
The fissure development pattern in the trending profile at the end of mining is depicted in
Figure 15a. The panel advanced from the right side (the opening-cut location) to the left (the stopping line), and as the buried depth increased, the fissures in the roof overburden gradually developed. The measurements indicate that in the ungrouted model of the trending section, the height of the caving zone was 18.91 m, and the height of the water-conductive fracture zone was 74.47 m. The maximum height of the water-conductive fracture zone was situated above the opening cut area. In the grouted model (
Figure 15b), upon completion of mining, the height of the caving zone was 13.82 m, and the height of the water-conductive fracture zone was reduced to 61.14 m. Similarly, the maximum height of the water-conductive fracture zone remained above the opening-cut area. These reductions in the height of the caving zone and water-conductive fracture zone indicate that the process of grouting the No. 4 aquifer effectively transformed the stratum’s properties and mitigated the damage from roof overburden. Moreover, the grouting modification caused a certain degree of hysteresis in roof damage [
36], decelerating the rate of roof degradation in comparison to the ungrouted scenario. Additionally, post-grouting modifications enhanced the overall integrity of the No. 4 aquifer and the weathering zone, ultimately increasing their strength [
37]. This improvement led to a decrease in the roof plate subsidence compared to the pre-grouting condition, which can consequently reduce surface subsidence to a certain extent.
Quantitative calculations were performed to determine the fractal dimensions of the overburden fissures at various mining stages, both before and after grouting. These calculations provided insights into the progression of the fracture generation, connection, and development induced by mining activities. In the numerical simulation of the trending profile, the evolution of the fractal dimensions of the fractures was analyzed by plotting them against the advanced distances before and after grouting, as shown in
Figure 15c. It was evident from the analysis that the fractal dimension graphs of both the grouted and ungrouted models exhibited characteristic distribution patterns, demonstrating three variable dimensional cycles and one steady dimensional stage throughout the coal seam mining process [
38].
Under the stress of the overlying rocks, geostress gradually concentrated at the opening cut and the foot of the quarry. When the geostress reached the compressive strength limit of the main roof, both the main roof and immediate roof broke, initially forming a caving zone. This marks the first “ascending–descending” dimensional cycle, as shown in
Figure 15c. With further panel advancement, the overlying rock layer bent and sank as a whole, creating the second “ascending–descending" dimensional cycle as the mudstone layer overlying the main roof broke and collapsed downward. This process also led to rapid development of fissures in the longitudinal direction. Subsequently, at this point, the fractal dimension of fractures reached its maximum value, marking the formation of the third “ascending–descending” dimensional cycle. As the panel continued to advance, fissures developed more prominently along the lateral direction. The fissures in the advancing area continued to develop and expand, while those in the central area gradually compacted. Eventually, the mining activities induced the overburden disturbance to reach a stable state, where the fissures on both sides of the quarry were more developed, and those in the central quarry were mostly compacted [
39]. During this stage, the fractal dimension curve stabilized, entering a phase of smooth fluctuation. It is worth noting that the fractal dimension of the fissures was slightly larger before grouting compared to after grouting, suggesting that the overlying fissures in the ungrouted model were more extensively developed, resulting in greater damage to the overlying rocks in the main roof.
4.5. Geophysical Validation and Analysis of the Mining Process
The geological column diagram of the 1010-1 panel indicated that mudstone and sandstone predominated in the 42 m overburden strata until the No. 4 aquifer's layers are encountered. The data collected from the drill holes were processed using a full-space laminar model, and a whole-space 3D resistivity inversion method was applied to obtain horizontal resistivity imaging maps at various heights for the main roof of this panel. Through this analysis, relatively low resistance zones were primarily identified based on apparent resistivity values less than 14 Ω·m.
Figure 16 shows the results of the inter-hole electrodynamics for detecting apparent resistivity at various elevations, depicting horizontal slices ranging from 5 m to 50 m on the roof of the 1010-1 panel. The apparent resistivity slices displayed in
Figure 16 revealed the presence of a predominantly low resistance area, which was primarily located amidst the sandstone and mudstone layers on the roof of the 1010-1 panel. This observation stems from the results of the inter-hole parallel electrical method exploration. From the integration of these findings with the geological data and on-site drilling observations, it was inferred that the low resistance area may be caused by the influence of grouting or fissure water within the sandstone layer on the roof. Furthermore, the resistivity slices at 45 m and 50 m on the roof portrayed the situation of the No. 4 aquifer within the management section. The majority of the regions in these slices exhibited high visual resistivity values and a low water content, indicating that the grouting transformation in this section had been successful.
According to the findings from the inter-hole parallel electrical method [
40,
41], the effectiveness of the grouting transformation in the overlying No. 4 aquifer and the weathering zone of the 1010-1 panel was evident. Although there were still localized areas with low resistivity values [
42], the majority of the area showed higher apparent resistivity values, which points toward a remarkable improvement resulting from the grouting process.
Table 2 presents the height calculation results of the safe coal–rock pillar in the 1010-1 panel using different methods. At the Wugou coal mine, a total of eight geological detection holes were drilled to measure the caving zone and water-conductive fracture zone on specific closed panels. The maximum measured caving height ratio of the neighboring 1016 panel was 4.69 times higher. Consequently, the caving zone’s height in the shallow area of the 1010-1 panel was determined to be 4.69 × 4.2 m = 19.70 m.
The 1010-1 panel was designed to mine up to an elevation of −262.96 m, where the underlying bedrock elevation is −240.11 m. The grouting transformation section of the No. 4 aquifer exceeded a thickness of 20 m. The actual upper limit elevation of this panel was −262.96 m. The actual minimum height of the collapse prevention pillar was measured at 43.19 m, surpassing the calculated values in
Table 2.
The stress monitoring data from the anchor bar at the track roadway and the working resistance data from the hydraulic support in the panel were analyzed. As the excavation of the 1010-1 panel progressed, the stress data from the track roadway anchor bar continued to change, as shown in
Figure 17. Prior to January 29, 2023, the stress level of the anchor bar at the wind roadway was relatively stable [
43]. However, as the 1010-1 panel advanced approximately 9.5 m, the stress on the anchor began to gradually increase due to the impact of mining on the surrounding rock at the roadway. The stress of the anchor at the track roadway increased rapidly at about 27.1 m of the panel advancement, reaching a peak at about 40 m of the panel advancement. Following this peak, the stress on the anchor suddenly decreased and stabilized rapidly. Moreover, the field measurements illustrated that none of the hydraulic supports reached their designed working pressures during the coal seam excavation in the grouted area.